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Well I did today with what I was going to do Saturday reclocked the turbo, adjusted the wastegate bracket and installed the oil drain flanges and the Turbosmart kompacts plumb backs. Disassembly went by fast but when I got to the wastegate bracket 2/3 screws were stripped. Managed to drill them out then use a hammer and screw driver to knock them loose. Got it all back together and it doesn't run nearly as loud now! Idle is much smoother doesn't sound like it's gonna take off.
Took it for a drive and I think @Boostking is going to be one happy tuner now. All boost surge is gone and with the kompacts in-between shifts are not as hard and it holds the boost there. I think we done did something good here boys. Will need to change the driver's drain from a PTFE fitting to a standard flex hose an fitting. Thought these lines were PTFE since my invoices say it but guess not. Still smoking after the drive but after me throwing that chra around a little today I wouldn't be surprised that it did smoke some right now.
Took it for a drive and I think @Boostking is going to be one happy tuner now. All boost surge is gone and with the kompacts in-between shifts are not as hard and it holds the boost there. I think we done did something good here boys. Will need to change the driver's drain from a PTFE fitting to a standard flex hose an fitting. Thought these lines were PTFE since my invoices say it but guess not. Still smoking after the drive but after me throwing that chra around a little today I wouldn't be surprised that it did smoke some right now.